WE Report

Lessons Learned

Lessons Learned865


Operator Rig Discipline / Origin Project Phase Well Section Date What Happened

DNO
6805 – DNO

Nobel Invincible Drilling Operational 2/6-7 S
Falstaff
Top hole 07/10/2024 Removed one slip element to allow passage of Frelok hydraulic line below RF without damage.

Lene Lomeland


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DNO
6758 – DNO

Nobel Invincible Drilling Operational 2/6-7 S
Falstaff
Top hole 23/09/2024 Movement of conductor. Adjusted scaffold at diverter platform. Installed chain hoist horizontally in . . .

Lene Lomeland


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DNO
6759 – DNO

Nobel Invincible Drilling Operational 2/6-7 S
Falstaff
Top hole 23/09/2024 The flowrate during cleanout of conductor was limited to 2000 lpm due to overflow of bird bath. . . .

Lene Lomeland


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DNO
6760 – DNO

Nobel Invincible Drilling Operational 2/6-7 S
Falstaff
Top hole 23/09/2024 During cleanout of conductor was filled with fluid. When drilling the drain hole the fluid poured . . .

Lene Lomeland


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DNO
6761 – DNO

Nobel Invincible Drilling Operational 2/6-7 S
Falstaff
Top hole 23/09/2024 Longer time than anticipated for grinding the weld on conductor.

Lene Lomeland


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DNO
6762 – DNO

Nobel Invincible Drilling Operational 2/6-7 S
Falstaff
Top hole 23/09/2024 Conductor sent out with metal protectors.

Lene Lomeland


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DNO
6763 – DNO

Nobel Invincible Drilling Operational 2/6-7 S
Falstaff
Top hole 23/09/2024 The hammer and drive sleeve were made up on the rig by Expro crew. The hammer and drive sleeve were . . .

Lene Lomeland


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DNO
6765 – DNO

Nobel Invincible Drilling Operational 2/6-7 S
Falstaff
Top hole 23/09/2024 After 2 ½ joints was driven in ground the rebound was observed to be very high, Blowcount was also . . .

Lene Lomeland


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DNO
6766 – DNO

Nobel Invincible Drilling Operational 2/6-7 S
Falstaff
Top hole 23/09/2024 Both TFMC and Mitsui numbers marked on joints. TFMC rig numbers marked but with prefix TFMC making . . .

Lene Lomeland


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Wellesley
6455 – Wellesley

COSLPromoter Drilling
Own Experience
Operational 35/10-12 S
Gnomoria
P&A 05/07/2024 Observed flowback of the mud lost while running and cementing 9 5/8″ casing. Of ±200 m3 of mud lost, . . .

Drilling Engineer / Morten Laget



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Wellesley
6456 – Wellesley

COSLPromoter Drilling
Own Experience
Operational 35/10-12 S
Gnomoria
P&A 05/07/2024 Discussion about the risk of accidentally pulling the seal assembly free (no outer lock ring . . .

Drilling Engineer / Morten Laget



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Wellesley
5936 – Wellesley

Deepsea Yantai Marine
Own Experience
Operational 35/10-10S
Carmen
CAN-Ductor 23/10/2023 Risk of WOW during Carmen CAN-Ductor installation and recovery leading to Wellesley being . . .

Stian Engvik / Morten Laget


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DNO
5912 – DNO

Deepsea Yantai Drilling
Own Experience
Operational 25/7-11 S
Norma
N/A 06/09/2023 Plugging of transfer lines when taking Microbar from vessels several times.

John Langelandsvik / Morten Laget


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DNO
5911 – DNO

Deepsea Yantai Drilling Operational 25/7-11 S
Norma
Reservoir section 05/09/2023 Time drill to initiate KO with 2 m/hr. Good performance kicking off from mainbore, no problems

Drilling Engineer / Morten Laget


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DNO
5852 – DNO

Deepsea Yantai Drilling
Own Experience
Operational 25/7-11 S
Norma
Top hole 30/07/2023 The pH meter showed indications of cement in return (pH value of 11.6-12.3). Due to poor visibility . . .

Drilling Engineer / Morten Laget


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DNO
5853 – DNO

Deepsea Yantai Drilling
Own Experience
Operational 25/7-11 S
Norma
Top hole 30/07/2023 After the cement of the 30″ conductor was set up the WHRT was released and POOH. Movement was seen . . .

Drilling Engineer / Morten Laget


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DNO
5855 – DNO

Deepsea Yantai Drilling
Own Experience
Operational 25/7-11 S
Norma
Top hole 30/07/2023 After the 30″ conductor shoe was drilled the inclination of the conductor increased. Used the WHRT . . .

Drilling Engineer / Morten Laget


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DNO
5859 – DNO

Deepsea Yantai Drilling
Own Experience
Operational 25/7-11 S
Norma
Top hole 30/07/2023 Drawwork in landing mode. No change in hookload while cementing and displacing.

Drilling Engineer / Morten Laget


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DNO
5861 – DNO

Deepsea Yantai Drilling
Own Experience
Operational 25/7-11 S
Norma
Top hole 30/07/2023 Difficult to see cement in return due to poor visibility at seabed. pH sniffer indicated cement in . . .

Drilling Engineer / Morten Laget


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DNO
5862 – DNO

Deepsea Yantai Drilling
Own Experience
Operational 25/7-11 S
Norma
Top hole 30/07/2023 When displacing the 26″ hole at TD a large volume of WBM was needed. And due to VDL the mud column . . .

Drilling Engineer / Morten Laget


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